Market Notices

116630GENERAL NOTICE15/05/2024 06:00:51 PM

Update - Network Augmentation Commissioned - QLD Region - 15/05/2024

AEMO ELECTRICITY MARKET NOTICE

Update - Network Augmentation Commissioned - QLD Region - 15/04/2024

Refer Market notice: 115974 and 116446

Guybal Munjan 275 kV Switching Station has been commissioned.

The former Ross - Chalumbin No. 857 and Ross - Chalumbin No. 858 275 kV lines have been replaced with the following lines:

H13 Ross - H93 Guybal Munjan No. 8916 275 kV line
H13 Ross - H93 Guybal Munjan No. 8917 275 kV line

H93 Guybal Munjan - H32 Chalumbin No. 857 275 kV line
H93 Guybal Munjan - H32 Chalumbin No. 858 275 kV line


Manager NEM Real Time Operations
116446GENERAL NOTICE02/05/2024 07:49:28 PM

Network Augmentation Commissioned - QLD Region - 02/05/2024

AEMO ELECTRICITY MARKET NOTICE

Network Augmentation Commissioned - QLD Region - 02/05/2024

Commissioned:

H13 Ross - H93 Guybal Munjan No.8917 275 kV line

Manager NEM Real Time Operations
116339POWER SYSTEM EVENTS26/04/2024 12:12:59 PM

Non-credible contingency event - NSW region - 26/04/2024

AEMO ELECTRICITY MARKET NOTICE.

Non-credible contingency event - NSW region - 26/04/2024

At 1112 hrs the Griffith to Darlington Point 132kV line (99K) and the Darlington Point BESS disconnected.

AEMO did not instruct load shedding.

AEMO observed 5 MW of electrical load lost.

The cause of this non credible contingency event is not known at this stage.

Manager NEM Real Time Operations
116329GENERAL NOTICE25/04/2024 11:56:40 AM

Planned outage of Gordon - Chapel St No. 1 220 kV line in the TAS region on 26/04/2024

AEMO ELECTRICITY MARKET NOTICE

The Gordon - Chapel St No. 1 220 kV line in the Tasmania (TAS) region is planned to be out of service from 1030 hrs on 26/04/2024 to 1500 hrs on 26/04/2024

A credible contingency event during this planned outage could cause a large reduction in generation in TAS.

Refer AEMO Network Outage Schedule (NOS) for further details.

Manager NEM Real Time Operations
116299POWER SYSTEM EVENTS24/04/2024 10:54:59 AM

Non-credible contingency event - QLD region - 24/04/2024

AEMO ELECTRICITY MARKET NOTICE.

Non-credible contingency event - QLD region - 24/04/2024

At 0855 hrs the Ross - Guybal Munjan 8916 275 kV line tripped at the Guybal Munjan end only.

AEMO did not instruct load shedding.

AEMO has not been advised of any disconnection of bulk electrical load.

The cause of this non credible contingency event has been identified and AEMO is satisfied that another occurrence of this event is unlikely under the current circumstances.


Manager NEM Real Time Operations
116276POWER SYSTEM EVENTS23/04/2024 12:09:41 PM

Non-credible contingency event - VIC region - 23/04/2024

AEMO ELECTRICITY MARKET NOTICE.

Non-credible contingency event - VIC region - 23/04/2024

At 1056 hrs the MOPS 11 Gen TX 2 Bus 500kV CB and the Dundonnell WF tripped.

AEMO did not instruct load shedding.

AEMO has not been advised of any disconnection of bulk electrical load.

The cause of this non credible contingency event has been identified and AEMO is satisfied that another occurrence of this event is unlikely under the current circumstances.

AEMO will not reclassify this event as a credible contingency event.


Manager NEM Real Time Operations
116162POWER SYSTEM EVENTS17/04/2024 06:10:18 AM

Update - Non-credible contingency event - VIC region - 17/04/2024

AEMO ELECTRICITY MARKET NOTICE.

Update - Non-credible contingency event - VIC region - 17/04/2024

Refer AEMO Electricity Market Notice 116160

At 0610 hrs the Heywood No 2 500 kV bus was returned to service.

The cause of this non-credible contingency event has been identified and AEMO is satisfied that another occurrence of this event is unlikely under the current circumstances.

AEMO will not reclassify this event as a credible contingency event.

Manager NEM Real Time Operations
116160POWER SYSTEM EVENTS17/04/2024 04:29:44 AM

Non-credible contingency event - VIC region - 17/04/2024

AEMO ELECTRICITY MARKET NOTICE.

Non-credible contingency event - VIC region - 17/04/2024

At 0414 hrs the Heywood No 2 500 kV bus tripped.

AEMO did not instruct load shedding.

AEMO has not been advised of any disconnection of bulk electrical load.

The cause of this non credible contingency event is not known at this stage.


Manager NEM Real Time Operations
116128GENERAL NOTICE15/04/2024 11:16:06 AM

SERVICE RESUMPTION- AEMO NEM Control Rooms BT Phones

AEMO ELECTRICITY MARKET NOTICE

SERVICE RESUMPTION - AEMO NEM Control Rooms BT Phones

Refer AEMO Electricity Market Notice 116127

AEMO advises participants that the service interruption relating to: AEMO NEM Control Rooms BT Phones has been resolved.
Participants may resume using the standard AEMO contact numbers.

Participants experiencing any further service issues should contact the AEMO Support Hub
Phone: 1300236600 Opt1
Email: supporthub@aemo.com.au

Manager NEM Real Time Operations
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